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Old 09-16-2008, 01:44 AM
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pifcat2 pifcat2 is offline
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Join Date: Jun 2003
Location: Willow Glen
Posts: 299
I removed most of the linkage, cleaned and greased it. The link bars weren't easy to pry off the ball ends. I didn't get the link bar off that's next to the throttle body because it started to bend. It appears to be spring loaded. I'll clean it as best I can and re-assemble tomorrow.

I disconnected the plug to the ICV while it was running and the idle dropped to under 1k until I restarted the engine. Seems to work fine.

I checked resistance on the micro switch with a voltmeter and it operated correctly. I noticed there is no adjustment on the switch body as it's held on a pin and screwed to the bracket. It's cable sheath on the connector mounted at the firewall side of the head was hard and a little frayed likely from the heat. The switch connector seems ok too and no obstructions to the switch.

I found this link for more info: High Idle 300E -88 (Have preformed search)
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'88 300TE, 175k, black RENNTech 3.6L Recaro C's AMG 1 SOLD
'92 500E, 110k, Spruce green, stock SOLD
'94 E320 Cabriolet, 130k, E500 wheels, Emerald green SOLD
'94 E320 Cabriolet, 110k, black, stock, SOLD
'88 300TE, 229k, dark grey, SOLD
'90 300CE, 212k, white, new paint, SOLD
'91 300E, 209k, white, rebuilt head SOLD
'74 914-6, grey, 2.7L 325hp twin turbo Audi conversion

Last edited by pifcat2; 09-16-2008 at 06:13 AM.
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