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Old 08-06-2015, 01:59 PM
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bsmuwk bsmuwk is offline
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Join Date: Jan 2009
Location: IL / WI
Posts: 1,013
I got a bit impatient last night and with a beer or three by me, I removed the engine harness (10 minutes) and rebuilt it (5 hours). All new wires, new plugs (I have a stockpile of them), and I reused the metal pins everywhere. All in all, I'm surprised anything was working correctly on the engine, wires were intertwined and somebody had a field day with electrical tape trying to solve some problems. Now I can start diagnosing any electrical problems the car is having, namely shutting off. It "seems" to run and start a bit better now, though it's probably just my butt scanner thinking the new harness actually might have done something positive.

I don't have any pictures of the harness I built (regretfully), but here are a bunch of pictures of the harness as I was digging into it and separating wires.

Now I have to figure out why the Shut Off Relay on the car is clicking. Joy.
Attached Thumbnails
OM603.971 - shimmy shimmy shimmy-071012_cookie_monster_featured120710144306.jpg   OM603.971 - shimmy shimmy shimmy-11231257_10207470780985668_2974225963681060991_n.jpg   OM603.971 - shimmy shimmy shimmy-img_4194.jpg   OM603.971 - shimmy shimmy shimmy-img_4195.jpg   OM603.971 - shimmy shimmy shimmy-img_4196.jpg  

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Allen Kroliczek
Oak Grove Autosport | Oak Grove Autosport
01 G500, 82 300TD, quite a few more.....
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