Confirmed problem--but not fixed
I disconnected the auxilliary pump and then hot-wired the mono valve so that it is closed when the ignition switch is on (bypassing the controller). The controller now works fine operating the blower speed and A/C clutch.
Apparently the controller output to the aux pump and mono valve is fried from the high pump amps (2.45A).
Next step is to replace the controller and re-connect the mono valve (leaving the aux pump disconnected).
Later on, I'll flush the cooling system and replace the aux pump. I think the idea of an in-line fuse for the pump is a good one. I'll probably do that.
Does anyone out there see any problems with my approach?
Thanks in advance.
Brent Smith
Atlanta, GA
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