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I'm concerned about doing that--originally I held it on with a generous strip of electrical tape and it didn't hold. The comm shaft with the worm gear generates a lot of torque, it pushes the plastic bushing retainer right out. I think it might be time to upgrade to duct tape and see how that holds. If that doesn't work I can just drill out the rivets, and tap the holes but thats a pain. |
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You are correct; there is a difference in the design of the sliding jaw over the years. In fact it got worse instead of better. Had about a 73 450SEL and needed to replace the sliding jaw. It was designed - believe it or not- so that it would come apart easily and the new sliding jaw could be installed without peening anything.
Why they changed this great design I will never know. |
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I still had to use a Dremel tool with a cutoff wheel to grind off the old peened part of the old pin and drive that pin out so that I could reuse the plastice pieces and the wavy washer. I will have to find someplace local where I can buy the clip as I did not buy the kit in the pic below. |
Yikes!
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I just fixed my left rear window which failed due to the white plastic slider breaking. To fix it I got a new slider from the junkyard (busted off the arm on the junkyard car, slider, rivet and all), ground off the rivet to get to the slider free, then drilled out the rivet on the arm in the car. I attached the new slider to my existing arm using a long set screw, two low-profile nuts and a bushing. I slightly drilled out the hole in the slider to fit the bushing, cut the bushing down so that it was just longer than the slider hole was deep and installed the bushing in the slider with some grease. I then took some red loc-tite and attached one nut just flush with the non-allen end of the set screw. After the loc-tite dried I slid the nut and setscrew into the slider and clipped the back onto the slider trapping the nut/setscrew assembly in it. I then put the slider into the window channel and installed the setscrew (now sticking out like a stud) into the hole in the arm that used to hold the rivet. Next I used the other nut, a wrench and an allen wrench to tighten down the assembly to the arm. I used SAE 1/4-20 hardware for everything.
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