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#1
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HELP Valve adjustment?
I did the valve adjustment and all were very tight. I suspected they had not been done for some time. (180,000m) So, After I do the adjustment the 300sd is hard to start and seems to be smoking much more.
The adjustment did make it run a little better, especially on take off. Is there a reason it is harder to start, before it would take half a crank and start now 2 to 4 cranks to get to start. What about the SMOKE?? |
#2
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will be a PITA but check them again!, if you didnt torque them tight enough they might be off, only way to be sure
if they are good then try diesel purge , change your fuel filters, check the air filter
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1985 300D - 599,xxxk - blue interior #265 Monark Nozzle, AL129X, 15" Ronals, Gen II Big Brakes hunting 1985 300D - 491,xxxk - in prog-{A-A IC, 3" exhaust, psi\pyro, 28*BTDC, Hella Euros, IP Limiter removal 1985 300TD - 783,xxxk - parts car,used new engine with ALDA cap inplace 1987 Kenworth T-600 8LL 425 CAT Mech. - 6,000,000+k - DEI exhaust wrap, punched through resonators, 1 recent rebuild, |
#3
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Also, make sure you reinstalled the "throttle" linkage correctly and that it's not binding.
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#4
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I changed the air filter 2 week ago when I got the car. Replaced a leaking fuel injector return line.
I was running a tank of B20 before changing Fuel filters. Can I get diesel purge locally? that was my next step. I initially was trying to solve a very low power situation. Car would have no GO under 30mph. After that it had a little more. |
#5
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Have you tried adjusting the ALDA?
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1984 300 Coupe TurboDiesel Silver blue paint over navy blue interior 2nd owner & 2nd engine in an otherwise 99% original unmolested car ~210k miles on the clock 1986 Ford F250 4x4 Supercab Charcoal & blue two tone paint over burgundy interior Banks turbo, DRW, ZF-5 & SMF conversion 152k on the clock - actual mileage unknown |
#6
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Do I adjust it while idling or do I just adjust a little then test drive?
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#7
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I know it sounds coincidental, but have you checked the glow plugs?
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RRGrassi 70's Southern Pacific #5608 Fairmont A-4 MOW car 13 VW JSW 2.0 TDI 193K, Tuned with DPF and EGR Delete. 91 W124 300D Turbo replaced, Pressure W/G actuator installed. 210K 90 Dodge D250 5.9 Cummins/5 speed. 400K |
#8
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You might consider checking for chain stretch and after that injection pump timing. I believe if all the valves were tight by adjusting them you have indirectly changed the effective timing. Thats why it might be smoking now. Just a suspicion combined with harder starts. This is a bit of a stretch but starting especially should have become easier.
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