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Old 11-20-2012, 11:00 PM
ah-kay ah-kay is offline
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Join Date: Mar 2009
Location: San Diego
Posts: 3,540
What a mess. What next?

Need some ideas here. I installed the head and torqued everything down. Before I put everything together, I decided to do a cold compression test and the result is NO good.

cyl 1 - 300
cyl 2 - less than 50.
cyl 3 - 350
cyl 4 - 200
cyl 5 - 300
cyl 6 - 100.

The engine was running but missing at idle. I should have done a compression test first before I pulled the head. I did not so I do not know what the reading was like. I did compression test on this engine 1 year ago and the result was good. I have a few questions:

1) How can cyl 2 be so low? The head is bad or the block? Put 2 spoonful of oil thru the inlet valve and the compression goes up a little bit to about 80.
2) Anything I can check before I pull the head again?
3) I have another #14 head. It is from the car where the oil pump chain snapped and buggered the engine. It is a good head as the car was running. Shall I try to install this head?
4) Can I reuse the Head Gasket? It is torqued down but never used so to speak.

Any help is appreciated.
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Not MBZ nor A/C trained professional but a die-hard DIY and green engineer. Use the info at your own peril. Picked up 2 Infractions because of disagreements. NOW reversed.

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Last edited by ah-kay; 11-21-2012 at 12:50 AM.
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