![]() |
|
|
|
#31
|
||||
|
||||
Quote:
__________________
" We have nothing to fear but the main stream media itself . . . ."- Adapted from Franklin D Roosevelt for the 21st century ![]() OBK #55 1998 Lincoln Continental - Sold Max 1984 300TD 285,000 miles - Sold The Dee8gonator 1987 560SEC 196,000 miles - Sold Orgasmatron - 2006 CLS500 90,000 miles 2002 C320 Wagon 122,000 miles 2016 AMG GTS 12,000 miles |
#32
|
||||
|
||||
Exhaust Gas Recirculator.
It has to do with reducing emissions. Tom W
__________________
[SIGPIC] Diesel loving autocrossing grandpa Architect. 08 Dodge 3/4 ton with Cummins & six speed; I have had about 35 benzes. I have a 39 Studebaker Coupe Express pickup in which I have had installed a 617 turbo and a five speed manual. ![]() ..I also have a 427 Cobra replica with an aluminum chassis. |
#33
|
|||
|
|||
Quote:
|
#34
|
||||
|
||||
What would the effect be of reducing the combustion chamber until the compression ratio were lets say 60 to one instead of 20? or 80 or 100? all of these possibilities exist up to the point of a full combustion chamber.
Tom W
__________________
[SIGPIC] Diesel loving autocrossing grandpa Architect. 08 Dodge 3/4 ton with Cummins & six speed; I have had about 35 benzes. I have a 39 Studebaker Coupe Express pickup in which I have had installed a 617 turbo and a five speed manual. ![]() ..I also have a 427 Cobra replica with an aluminum chassis. |
#35
|
||||
|
||||
Quote:
Tom W
__________________
[SIGPIC] Diesel loving autocrossing grandpa Architect. 08 Dodge 3/4 ton with Cummins & six speed; I have had about 35 benzes. I have a 39 Studebaker Coupe Express pickup in which I have had installed a 617 turbo and a five speed manual. ![]() ..I also have a 427 Cobra replica with an aluminum chassis. |
#36
|
|||
|
|||
Quote:
It can only bend at the point where the combustion chamber is just slightly overfilled. Are you thinking that the rod will bend under a compression ratio of 80:1? I haven't pondered that one..........but, I think the rod is strong enough to survive that. |
#37
|
|||
|
|||
Quote:
However, if you believe the rod will bend at 60:1 or 80:1 compression, that's a completely different scenario. I'd need to study it a bit more. |
#38
|
|||
|
|||
One other point of note to completely dispel this theory:
M/B changed the design of the connecting rods for the later engines. Clearly, if they identified a head gasket leak as the culprit, they would have addressed this problem. The fact that they redesigned the rods tends to point to a fatigue issue in the rods rather than a failure caused by external influences. Furthermore, a slightly redesigned rod won't dramatically reduce the failure rate caused by your theory. Sure, it's got a bit more capability, but if it can't withstand 80:1 compression, the new rod is not likely to withstand 90:1 compression. I don't think we've got sufficient data on the new rods to make any conclusions as to their success or not........however. |
#39
|
||||
|
||||
Several folks have reported bent rods here with the replacement blocks with the "upgraded" rods.
Tom W
__________________
[SIGPIC] Diesel loving autocrossing grandpa Architect. 08 Dodge 3/4 ton with Cummins & six speed; I have had about 35 benzes. I have a 39 Studebaker Coupe Express pickup in which I have had installed a 617 turbo and a five speed manual. ![]() ..I also have a 427 Cobra replica with an aluminum chassis. |
#40
|
|||
|
|||
That would definitely help your case. Who are these folks.........I'd be curious if any symptoms of head gasket failure would be evident?
|
#41
|
||||
|
||||
Quote:
Tom W
__________________
[SIGPIC] Diesel loving autocrossing grandpa Architect. 08 Dodge 3/4 ton with Cummins & six speed; I have had about 35 benzes. I have a 39 Studebaker Coupe Express pickup in which I have had installed a 617 turbo and a five speed manual. ![]() ..I also have a 427 Cobra replica with an aluminum chassis. |
#42
|
||||
|
||||
Quote:
If benz did not know for sure what was causing the problem the upgraded rods may have been an easy to do solution with no assurance of success. We do know that all 3.5 versions suffer the bending rod syndrome, I believe, so benz eventually solved the problem by going back to the trusty 3.0 block with four valve heads. This supports in my mind the theory that the 3.5 block flexed too much. If there were nothing wrong with the 3.5 block why would they go back to the 3.0? Tom W
__________________
[SIGPIC] Diesel loving autocrossing grandpa Architect. 08 Dodge 3/4 ton with Cummins & six speed; I have had about 35 benzes. I have a 39 Studebaker Coupe Express pickup in which I have had installed a 617 turbo and a five speed manual. ![]() ..I also have a 427 Cobra replica with an aluminum chassis. |
#43
|
|||
|
|||
Quote:
There is no question that the 3.5 block is not stiff enough when the proximity of the cylinders is observed. In fact, the 3.0 block tends to violate the typical spacing distances that are considered "normal". Whether this lack of stiffness translates into a head gasket failure (no data) and that it further cascades into a connecting rod failure (no data) is a real stretch, IMHO. Last edited by Brian Carlton; 03-24-2008 at 11:17 PM. |
#44
|
||||
|
||||
Who spoke of a rod bearing failure? I did not, but if a rod is bent I would want to replace the rod bearing too.
And as far as data, is there any data to support any of our theories about the cause of rod bending? Tom W
__________________
[SIGPIC] Diesel loving autocrossing grandpa Architect. 08 Dodge 3/4 ton with Cummins & six speed; I have had about 35 benzes. I have a 39 Studebaker Coupe Express pickup in which I have had installed a 617 turbo and a five speed manual. ![]() ..I also have a 427 Cobra replica with an aluminum chassis. |
#45
|
|||
|
|||
Quote:
Nope..........all gas.........no data. But your theory is especially weak because of the lack of any anecdotal evidence to support the head gasket. If the head gasket fails, there are symptoms to support that failure..........you have none. |
![]() |
Bookmarks |
|
|