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W201 EHA adjustment
Well I did it, ran better, put some Irridium plugs in it, and in less then a day it misses all over the place, runs really lean at the bottom end (O2 gauge tells me this).
As soon as this started I pulled the Irridiums, and put the coppers back in, cranked the EHA back to it's stock position. This didn't affect the car at all. Had my mechanic run a smoke test, replaced the rubber boot below the A/F meter it had a slight leak, still no improvement. Mech ran a compression test 98 125 150 100. It's hard for me to make any correlations in running behavior right now as I'm f'in pissed. However assuming the plugs stressed the engine a little more, say a blown head gasket are these compression number bad enough that I should consider a rebuild? Any suggestions? 1987 4 cyl 8V 5 speed M102 motor
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Davo 500sl R107 |
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