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W201 EHA adjustment
Well I did it, ran better, put some Irridium plugs in it, and in less then a day it misses all over the place, runs really lean at the bottom end (O2 gauge tells me this).
As soon as this started I pulled the Irridiums, and put the coppers back in, cranked the EHA back to it's stock position.
This didn't affect the car at all.
Had my mechanic run a smoke test, replaced the rubber boot below the A/F meter it had a slight leak, still no improvement.
Mech ran a compression test 98 125 150 100.
It's hard for me to make any correlations in running behavior right now as I'm f'in pissed.
However assuming the plugs stressed the engine a little more, say a blown head gasket are these compression number bad enough that I should consider a rebuild?
Any suggestions?
1987 4 cyl 8V 5 speed M102 motor
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Davo
500sl R107
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