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Well I just ran it again... this time I electrical taped around the boot on the offending plug wire and it ran near perfect. The miss was 99% gone. I still hear that it could be a slight bit stronger and smoother. I'm going to tape around the wires too since I saw a voltage leak on the insulation when I watched in the dark last night. That should cure it for now. I'm not sure how long term this fix will be but I wanted to figure out that this is the fix before I put a dollar more into the car.
And weird... but the smoke was gone. That's nice! But I wonder if it will come back after running for a bit. It was on and off before. I'm a little baffled by it.
What's interesting is that this car has as much get up and go on 4 and 5 cylinders as my OM603 in my 87 300d has on all 6 with the ALDA removed. Kind of fun to drive after the car is running right.
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-E300d '99 350k
-Suburban '93 220k
-TDI Jetta '03 350k
Sold
-F250 '96 7.3
-Dodge Ram 12V
-E320 '95 200k
-E320 Wagon 1994 155k
-300d Turbo '87 187k miles
-E320 1994 200k
-300d Turbo '84 245k (sold to Dan62)
-300d Turbo '84 180k
-300sd '80 300k
-7.3 Powerstroke Diesel 15P Van 500k+ miles
-190d '89 Non Turbo 2.5 5cyl 240k (my first MB)
Tom's Imports of Columbia MO Ruined the IP in changing leaky delivery valve O-Rings - Refused to stand behind his work. Mid-MO MB drivers-AVOID Tom's.
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