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#1
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Did you replace the little pre-filter at the same time?
If so did you happen to put an o-ring on it? When I changed all my lines I put fuel in each line to offset some of the cranking issues
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raMBow 1999 E300DT Obsydian Black Metallic, Heated Full Leather Parchment options, E2, K2, 136,000+, best 36.5 mpg - GP's 12-04 & 11-12 Zero Stuck 2010 Honda Odyssey - The BrideMobile - best 26.5 (2) 2005 Honday Accord- (1 -Corporate 1 - Personal) - 110,000 4-cyl 30mpg 2000 VW Golf GLS TDI, Upsolute Chip (sold to Brother, now 300+k on it) 48.5 mpg like clock work 1987 Honda CRX HF - Sold 87,000 always over 50 mpg Max 67 mpg |
#2
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Quote:
got it fixed..that was the problem. i took the lines off and inspected the fit and the noticed the prefilter hose wasnt very snug. compared it to the old line and it was missing the 0-ring. thanks for the help guys i spent whole days on that lil project
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1993 e300 1995 e320 1994 e320 2006 s500 4matic 2004 Jeep wj overland 2001 Ducati 748 2004 Honda shadow aero |
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