![]() |
|
|
|
|
![]() |
|
LinkBack | Thread Tools | Display Modes |
|
#1
|
||||
|
||||
bummed.... engine running but accessories not turning. 1982 300CD Turbo
got to work this morning and had an alt light and no power steering. the sinking feeling in the pit of my stomach said sheared crank. I verified it under the hood but have not removed anything, I am still at work. I am going to have the wife pick me up and go get the trailer to take it home. whats the best and worst I can expect? is it simply a key or is there some other big problem lurking?
found this thread, hopefully it is just the cap screws Engine running; no belts turning, no pulleys turning
__________________
![]() 1982 300CD Turbo (Otis, "ups & downs") parts for sale 2003 TJ with Hemi (to go anywhere, quickly) sold 2001 Excursion Powerstroke (to go dependably) 1970 Mustang 428SCJ (to go fast) 1962 Corvette LS1 (to go in style) 2001 Schwinn Grape Krate 10spd (if all else fails) Last edited by lutzTD; 09-29-2009 at 08:29 AM. |
#2
|
|||
|
|||
Now I'm bummed too, good luck you'll get it!
__________________
1982 300SD |
#3
|
|||
|
|||
Not an uncommon problem on 617's. Should be fixable. Even if the pin slots on the crank nose are bad, new pin holes can be drilled.
__________________
1977 300d 70k--sold 08 1985 300TD 185k+ 1984 307d 126k--sold 8/03 1985 409d 65k--sold 06 1984 300SD 315k--daughter's car 1979 300SD 122k--sold 2/11 1999 Fuso FG Expedition Camper 1993 GMC Sierra 6.5 TD 4x4 1982 Bluebird Wanderlodge CAT 3208--Sold 2/13 |
#4
|
|||
|
|||
I lost an alternator key once. Though the alternator sized. Lost the pulley and everything. (going from San Francisco to Elko, Nv. it happened on 80 outside Fallon NV) Got towed back to Elko pulled the Alternator. It was a $10 fix. new key and pulley. Never figured out why. But it was good t go.
Hopefully it will be a relatively easy fix. Good luck.
__________________
92 300D 2.5L OM602 OBK #59 |
#5
|
||||
|
||||
well its the worst. the keys on the crank nose are bunged along with the id of the balancer. I am going to go get a new balancer from the pnp, not sure how much material is gone from the crank nose. when drilling new holes, is the hardness of the crank and balancer similar? is it better to drill new holes or enlarge the current ones?
__________________
![]() 1982 300CD Turbo (Otis, "ups & downs") parts for sale 2003 TJ with Hemi (to go anywhere, quickly) sold 2001 Excursion Powerstroke (to go dependably) 1970 Mustang 428SCJ (to go fast) 1962 Corvette LS1 (to go in style) 2001 Schwinn Grape Krate 10spd (if all else fails) Last edited by lutzTD; 11-23-2011 at 08:36 PM. |
#6
|
|||
|
|||
There are a couple of threads which describe drilling the crank. My recollection is that the new holes were drilled 90 degrees away from the existing ones.
__________________
1977 300d 70k--sold 08 1985 300TD 185k+ 1984 307d 126k--sold 8/03 1985 409d 65k--sold 06 1984 300SD 315k--daughter's car 1979 300SD 122k--sold 2/11 1999 Fuso FG Expedition Camper 1993 GMC Sierra 6.5 TD 4x4 1982 Bluebird Wanderlodge CAT 3208--Sold 2/13 |
#7
|
||||
|
||||
Yikes....how tight did you have the belt tension set? I keep mine all quite loose to prevent this issue....
__________________
-diesel is not just a fuel, its a way of life- ![]() '15 GLK250 Bluetec 118k - mine - (OC-123,800) '17 Metris(VITO!) - 37k - wifes (OC-41k) '09 Sprinter 3500 Winnebago View - 62k (OC - 67k) '13 ML350 Bluetec - 95k - dad's (OC-98k) '01 SL500 - 103k(km) - dad's (OC-110,000km) '16 E400 4matic Sedan - 148k - Brothers (OC-155k) |
#8
|
|||
|
|||
Does belt tension have any effect? I'm pretty sure MB knew there was a weakness and if my memory serves me correctly, even recalled the early W116 SD turbo engines because they were throwing off their balancers.
Any idea why it failed in this instance?
__________________
1977 300d 70k--sold 08 1985 300TD 185k+ 1984 307d 126k--sold 8/03 1985 409d 65k--sold 06 1984 300SD 315k--daughter's car 1979 300SD 122k--sold 2/11 1999 Fuso FG Expedition Camper 1993 GMC Sierra 6.5 TD 4x4 1982 Bluebird Wanderlodge CAT 3208--Sold 2/13 |
#9
|
|||
|
|||
What corrective action was taken in conjunction with the recall?
|
#10
|
|||
|
|||
Possibly locktight on any fastenings? They have been known to loosen off I think. Miserable experience to have. Especially if damage has occured.
I cannot think of anything else they might have done during the recall except perhaps harder pins as well if they suspected shearing was an issue. |
#11
|
|||
|
|||
Quote:
Haven't been able to find anything. Can't remember where I read about the recall.
__________________
1977 300d 70k--sold 08 1985 300TD 185k+ 1984 307d 126k--sold 8/03 1985 409d 65k--sold 06 1984 300SD 315k--daughter's car 1979 300SD 122k--sold 2/11 1999 Fuso FG Expedition Camper 1993 GMC Sierra 6.5 TD 4x4 1982 Bluebird Wanderlodge CAT 3208--Sold 2/13 Last edited by kerry; 09-29-2009 at 03:50 PM. |
#12
|
||||
|
||||
yeh looks like I will drill 2 holes 90 degree off. The engine was making a clattering noise for 3 weeks. I searched and searched and couldnt find it. I finally decided it was the motor mounts. looks like that guess was wrong. I think the last straw was turning the engine by the crank bolt to do the valve adjust and my own inexperience with these engines. the bolt was loose when I was turning the motor over, but it didnt clue me to the bigger issue, I just retightened it
__________________
![]() 1982 300CD Turbo (Otis, "ups & downs") parts for sale 2003 TJ with Hemi (to go anywhere, quickly) sold 2001 Excursion Powerstroke (to go dependably) 1970 Mustang 428SCJ (to go fast) 1962 Corvette LS1 (to go in style) 2001 Schwinn Grape Krate 10spd (if all else fails) |
#13
|
||||
|
||||
![]() Any chance the balancer had been pulled off by a mechanic recently?
__________________
http://superturbodiesel.com/images/sig.04.10.jpg 1995 E420 Schwarz 1995 E300 Weiss #1987 300D Sturmmachine #1991 300D Nearly Perfect #1994 E320 Cabriolet #1995 E320 Touring #1985 300D Sedan OBK #42 |
#14
|
||||
|
||||
Quote:
no, I had some wicked vibes from the transmission for a long time until I fixed it a while back. From what I have read the failure path is: Vibration from bad/old mounts causes the bolt to come loose which in turn allows the dowels to move making their fits progressively looser until they finally shear. I had noticed more noise from the engine that disappeared at 900 RPM, looking back it must have been the balancer making the sound. Since I had no idea this was an issue, I am used to working on US V8's, I did not even think to check the balancer bolt. I noticed it was loose, which was I guess my last chance to fix it, when I did the valves 2 weeks ago. I should have torqued it then but I tightened it and forgot about it. seems like a poor design for a joint, but I guess if all is right it will last a long time. not sure why they didnt just make the crank snout longer. I rule of thumb for a good shaft fit is 1.5 times the diameter for the length of engagement. this one is not long enough to be a good joint.
__________________
![]() 1982 300CD Turbo (Otis, "ups & downs") parts for sale 2003 TJ with Hemi (to go anywhere, quickly) sold 2001 Excursion Powerstroke (to go dependably) 1970 Mustang 428SCJ (to go fast) 1962 Corvette LS1 (to go in style) 2001 Schwinn Grape Krate 10spd (if all else fails) |
#15
|
||||
|
||||
I'm not sure why they used round keyways, maybe because the section at the shear line is maxxed out without weakening the hub much. The way that they fail is that folks pull the harmonic balancer and bugger up the pin holes when they reinstall.
I am skeptical of drilling new holes successfully because getting a precise hole seems very very difficult to me. When I had the wobbling hb my favorite machinist advised me to get another crank. If he couldn't drill a proper new keyway I don't see how a hobbiest can do it in their garage with hand tools. It doesn't hurt to try though. The alternative is to tear down the entire motor and put in a new or good used crank. Just the labor to tear it down and reassemble is probably 2K.
__________________
[SIGPIC] Diesel loving autocrossing grandpa Architect. 08 Dodge 3/4 ton with Cummins & six speed; I have had about 35 benzes. I have a 39 Studebaker Coupe Express pickup in which I have had installed a 617 turbo and a five speed manual. ![]() ..I also have a 427 Cobra replica with an aluminum chassis. |
![]() |
Bookmarks |
|
|