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#1
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OM 606 Drilled too deep trying to extract a stuck Glow Plug
Hi Guys.
I know stuck Glow plugs in the 606 has been discussed endless. But here is a new one: As the title suggests I drilled too deep when trying the extraction process. I was following the method where you tap the body of the GP so you can install a hardened bolt into the body and slide it out by tightening a nut down the bolt. But I never got that far. When I was drilling out the center of the GP, I must have went right through the tip on the GP. I went so deep that fuel started to flow up into the Glow Plug chamber. What is behind there? Did I just completely ruin this head, thereby ruining this car? By the way GP still stuck in there. The tap/bolt puller method didn't work for me. Thanks in advance.
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Mike Mass Freehold, NJ 1999 E300 TD 178,000 miles 2007 E320 Bluetec - Sold 1998 E300 TD - R.I.P. ![]() |
#2
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you would have had to drilled through the aluminium head material to hit the injector. even then, not much fuel would come out and i would have been very difficult to drill through.
more likely, and much more seriously, it may have been coolant! Pull the injector. thats only reasonable next step after checking with a good light source if you can see the "mixing' ball in the prechamber through your drilled hole. |
#3
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Ouch. I'm not sure what is in line with the glows on the 606, but are you sure it is not coolant?
I'd guess you can put a fork in that head...unless you got lucky and drilled into one of your injectors?
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RenaissanceMan Labs: where the future is being made today. Garage: 2017 Chevy Colorado Diesel (nanny state emissions) 2005 Volvo S40 T5 AWD, 77k 1987 Mercedes-Benz 300D turbodiesel, 4 sp auto, 156k - 28.7 mpg 1996 Tracker 4x4, 2 door, 16v, 3 sp auto. 113k - 28.6 mpg WARNING: this post may contain dangerous free thinking. |
#4
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Im almost 100% sure it's fuel.
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#5
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Now you guys have me doubting myself. I certainly know the difference between diesel fuel and antifreeze. But the entire garage had already stunk of fuel, PB Blaster, WD 40, etc from doing this. When I drilled through too deep and the fluid filled up the GP port, I went with the assumption I drilled right thru the tip of the GP and I saw fuel.
But I guess it is possible I wasn't drilling perfectly straight and went through the wall of the aluminum head. Let's stick with the assumption it is fuel. If that is the case, what is just beyond the tip of the GP? Because at this point I am thinking of retreading the port, plugging it up and run on just 5 GP's. My concern with this is that clearly fragments of the GP (metal shavings, broken ceramic tip, etc) will be left in there, If I drilled straight back too deep what else could I have damaged? Will these fragments fall into vital areas of the engine like the cylinder, pistons, etc?
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Mike Mass Freehold, NJ 1999 E300 TD 178,000 miles 2007 E320 Bluetec - Sold 1998 E300 TD - R.I.P. ![]() |
#6
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I would pull the injector to find out. At minimum, you can find out if the glow plug tip is still in there.
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![]() All Diesel Fleet 1985 R107 300SLD TURBODIESEL 2005 E320 CDI (daily) LOTS of parts for sale! EGR block kit http://www.peachparts.com/shopforum/diesel-discussion/355250-sale-egr-delete-block-off-plate-kit.html 1985 CA emissions 617 owners- You Need This! Sanden style A/C Compressor Mounting Kit for your 616/ 617 For Sale + Install Inst. Sanden Instalation Guide (post 11): http://www.peachparts.com/shopforum/diesel-discussion/367883-sanden-retrofit-installation-guide.html |
#7
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There is not enough fuel available in the injector to fill up the glow plug port. It would have to fill up the pre-chamber and the cylinder before it flowed out of the GP hole.
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Greg 2012 S350 BlueTEC 4Matic 2007 ML 320 CDI 2007 Leisure Travel Serenity 2006 Sprinter 432k 2005 E320 CDI 1998 SLK230 (teal) 1998 SLK230 (silver) 1996 E300D 99k, 30k on WVO Previous: 1983 240D, on WVO 1982 300D, on WVO 1983 300CD, on WVO 1986 300SDL 237k, 25k on WVO (Deerslayer) 1991 350SDL 249k, 56k on WVO - Retired to a car spa in Phoenix 1983 380 SEC w/603 diesel, 8k on WVO 1996 E300D 351k, 177k on WVO |
#8
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The injector is made out of steel. Not sure of its Rockwell hardness, but pretty sure you would have to put some 'umph' into your drilling to go through it. Even if you hit the injector, there's a tiny amount of fuel in it, and even if the fuel could "flow" through it just sitting there, not sure there's enough in the line to somehow weep downwardly, although gravity would certainly move whatever fuel from high to low. Take a paper towel to sop up the fluid and then do a smell test. I agree a little bit of diesel or other similar fluids can stink up the garage where everything stinks like diesel, especially once it gets atomized and in the air.
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#9
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So, regards the GP drillout; is a helicoil installation, part of the possible plan going forward?
At what point do you, (generic you) go with a new head assembly? Just trying to explore your ultimate options going forward on completely solving this job.......
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'06 E320 CDI '17 Corvette Stingray Vert Last edited by Skid Row Joe; 04-11-2016 at 06:41 PM. |
#10
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depending on where this thing broke off (I think the threaded portion came out, leaving just the long shaft on the GP?) would depend on whether the threads would need to be reconstructed.
I'm going to venture a guess and say that a leakdown would be pointless...if there is coolant pouring out, the jacket has been breached. At this point the injector needs to be pulled, and a scope inserted through both the GP and injector holes to asses the damage. From there, post up the pictures and we will all mull over the best solution. If the only alternative to an unconventional repair like I detailed is replacing the head, which the OP says is not an option, then we should get creative! If nothing else, we will gain knowledge of what the options for repairs are as this type of thing becomes more common as more GPs fail in the 606 engine out there.
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RenaissanceMan Labs: where the future is being made today. Garage: 2017 Chevy Colorado Diesel (nanny state emissions) 2005 Volvo S40 T5 AWD, 77k 1987 Mercedes-Benz 300D turbodiesel, 4 sp auto, 156k - 28.7 mpg 1996 Tracker 4x4, 2 door, 16v, 3 sp auto. 113k - 28.6 mpg WARNING: this post may contain dangerous free thinking. |
#11
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I don't think the injector is inline with the glow plug.
Beyond the tip of the glow plug is the opposite side of the pre-chamber and then the head casting. If you could drill through the pre-chamber wall, you would hit coolant.
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-Evan Benz Fleet: 1968 UNIMOG 404.114 1998 E300 2008 E63 Non-Benz Fleet: 1992 Aerostar 1993 MR2 2000 F250 |
#12
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Quote:
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85 300D turbo pristine w 157k when purchased 167,870 July 2025 83 300 D turbo 297K runs great. SOLD! 83 240D 4 spd manual- parted out then junked |
#13
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Ugh. It's more than a 'little' fluid. I guess I am mistaken and I really stuck coolant. So head is shot if that's the case? Can't just plug up the hole and run it on 5 GP's?
I will pull the injector and do the smell test to double check. But it sounds like you guys have convinced me. If the head is shot I am going to just sell the car for parts at this point. I have no one to do a head replacement for me and if I can't even handle changing some GP's, I certainly am not going to try and tackle a head removal.
__________________
Mike Mass Freehold, NJ 1999 E300 TD 178,000 miles 2007 E320 Bluetec - Sold 1998 E300 TD - R.I.P. ![]() |
#14
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Per dimensions of the glow plug in this ebay listing
28 mm is the portion of the tip that extends into the pre-combustion chamber, from the flare to the glow plug hex (assumed where it snapped off) is about 2 x 28 mm. 56 mm is 2.2 inches. Did you drill more than 2 inches deep?
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85 300D turbo pristine w 157k when purchased 167,870 July 2025 83 300 D turbo 297K runs great. SOLD! 83 240D 4 spd manual- parted out then junked |
#15
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Quote:
Quote:
Sounds like it was just about that length.
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Mike Mass Freehold, NJ 1999 E300 TD 178,000 miles 2007 E320 Bluetec - Sold 1998 E300 TD - R.I.P. ![]() |
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